Philip Morris
(Active) Production Department Control & Improvement Plan
Fields
- Type
- REPT, REPORT, OTHER
- CHAR, CHART, GRAPH, TABLE, MAPS
- Area
- JENKINS,DEBBIE/OFFICE
- Characteristic
- ILLE, ILLEGIBLE
- MARG, MARGINALIA
- Named Organization
- Scanpro
- Thermo Electron
- Named Person
- Ampey, D.
- Bailey, B.
- Ballard, G.
- Bandy, J.
- Barrington, J.
- Bohon, R.
- Braswell, R.
- Brown, J.
- Budd, D.
- Bullock, T.
- Clark, D.
- Clarke, W.E.
- Claxton, S.
- Cummins, B.
- Darrah, S.
- Deck, J.
- Donaher, D.
- Dudley, P.
- Duncan, F.
- Estes, B.
- Evans, J.
- Evers, D.
- Garg, R.
- Glass, J.
- Greenburg, P.
- Hall, D.
- Hall, R.
- Hanks, J.
- Harrison, C.
- Hartsell, C.
- Hayes, W.
- Hensley, J.
- Jackson, L.
- Jenkins, D.
- Jones, G.
- Jones, J.
- Little, T.
- Lusk, J.
- Mayes, B.
- Mcfee, F.
- Mclaughlin, I.
- Mertz, D.
- Mitchem, D.
- Narron, J.
- Nelson, S.
- Orms, D.
- Pitts, P.
- Puglisi, P.
- Saunders, D.
- Shakeri, S.
- Sharkey, J.
- Shope, B.
- Stephenson, D.
- Tiller, M.
- Timpano, A.
- Tudor, A.
- Wagner, R.
- Waltman, H.
- Webb, T.
- Williams, W.
- Worrell, B.
- Wyche, B.
- Bailey, B.
- Document File
- 2024794524/2024794872/Sp Operating Problems Worklife
- Issues Principles Nonconformances
- 2024794736/2024794871/T0913 0.080
- Issues Principles Nonconformances
- Litigation
- Stmn/Produced
- Master ID
- 2024794814/4827
Related Documents:- 2024794814 Pdmt C&I Plan and Resource Allocation
- 2024794821-4823 Resource Allocation List Production Personnel Salaried
- 2024794824 Resource Allocation List Production Personnel Hourly
- 2024794825 Resource Allocation List Non-Production Personnel Salaried
- 2024794826 Resource Allocation List Non-Production Personnel Hourly
- 2024794827 Resource Allocation List Non-Production Personnel Salaried
- Site
- M45
- Date Loaded
- 31 Jan 1999
- UCSF Legacy ID
- hbd73e00
Document Images
(ACTIVEI
PRODUCTION DEPARTMENT-
CONTROL & IMPROVEMENT PLAN
DATE: 11'09 92
STA(17 TEAM I.EADEKt';
N UATL? NROBLEJb1
; . :IE3LNCE i . .;:
. ;.06JECTIVa=
TEAM MEMBE 5
(ACCC3UN't'ABLE
PDCA'tiildELINE
1 02/15/91 LINE III BLENDING - WEIGH NOV.'91 - JAN.'92 TQM's MAINTAIN WEIGHBELT SET B. ESTES D.
BUDD/B.ESTES P 2/15/91
BELT SET POINTS ARE OFF POINTS ON STANDARD AND F. DUNCAN D:
STANDARD A HIGH KEEP BLENDING FEED J. BROWN C-
PERCENTAGE OF THE TIME PARAMETERS IN CONTROL F. McFEE A-
M. Tiller IRes./ l1 1/1 6:NEXT MTG
(MAY CHANGE DUE TO NEW TM) 1211 4UPDA-T-E PDF.1Ti
? 01 / 10_ /92 TOBACCO RAW MATERIALS TEST RUN IN 12/91 DETERMINE MAJOR CAUSES R. WAGNER D_ . ORMS/B.
S_ /B. ESTES P- 1/1 3i92
ARE BEING LOST FROM THE SHOWED 1.47% OF TOTAL AND RECLAIM 70% OF CURRENT C. HARRISON D- 6, 1i92
PROCESS IN LINE I INFEED POUNDS WERE RAW MATERIAL PRESENTLY B. WORRELL C 81 92
BLENDING BEING LOST BEING DISCARDED D. BUDD A- 1 i28f93
(ON SCHEDULE'
3 0;t;05!92 LINE I BLENDING 1, VARIED TYPES OF RAW MAT- IMPLEMENT SHORT AND A. TIMPANO B. ESTES P-
2'17 92
WORKLIFE ISSUES: ERIAL CONTAINERS (PM80S, LONG TERM SOLUTIONS TO D. ORMS D~ 3'15!92
1. CONGESTION HHDS, WIREHEADS, SM.CASES) ALLEVIATE THESE PROBLEMS D. HALL C 10 15:92
2. ERGONOMIC PROBLEMS 2. STRIPPING & BREAKDOWN R. BOHON A- 7;31:93
3. PHYSICAL WORKLOAD DUE AT 12 DIFF. LOCATIONS P. GREENBURG_
TO INCREASED THRU-PUT 3. INCREASED MACHINE (ON SCHED_ ULE)
SPEED LI & LII
19 __ ~_
2/91
EXCESS FOAM ON TOP OF
Iv11CR0 ACTIVITY AROUND
INSTALL A FOAM CONTROL
S. SHAKERI
D. SAUNT)ERS
P 2/15/91
LINE I & II MACHINE ROOM FOAMING AREAS SHOWER SYSTEM ON THE D 2/30/91
SBW CHEST SBW CHESTS C 3'22'91
A 9'4;91 luIl
1L11 COMPLETE)
C 7i20:92 (LI)
A 9!31,'92 (LI)
ICOMPLETE EXCEPT FOR
PLATFORM NEEDED TO_
CLEAN PLUGGED
NOZZLESI
22 2/10/92 TOM REVIEW & ROUTINE REASONS GIVEN ON TQM AND PROVIDE REASONS FOR UPWARD D. MERTZ D.
SAUND_ERS_ P
PROCESS HIGH FLOWS ARE NOT REPEATED REQUESTS FOR PC TRENDS IN TOM WWT FLOWS W. E. CLARKE D
ACCOUNTED FOR BY PROD GROUP TO FIND OUT REASONS SONS FROM PROCESS AND PROVIDE C- 6;8,'92
PERSONNEL AND REASONS SYSTEM TO INVESTIGATE BY A- 12/28/92
ARE UNCLEAR
PROD PERSONNEL ~
IDEBUGGING NEU
--
TRANSMITTEFa
24 3/2/92 MANY ACTIVITIES REQUIRED TO_ WET FELT CHANGE PROCEDURE DECREASE THE NUMBER OF HIGH J.
HENSLEY _ D. SAUNDERS 12,'31*' A
CHANGE CONTINUOUS WET RISK ACTIVITIES REQUIRED W. E. CLARKE (ON SHCEDUL 0
FELTS PLACE EMPLOYEES AT TO CHANGE THE WET FELT W. HAYES UPDATE ATE TO P~1P
GREAT RISK OF INJURY MACHINE ROOM 12/1d+~2K2
SUPVS. ~ CD
(c,ln/xI/iccnolplan)
IS ZS v E; 4.ty zt)z
i

(ACTIVE)
PRODUCTION DEPARTMENT
CONTROL & IMPROVEMENT PLAN
DATE: 11 09 9-
sTAR'r TEAM LEAD$Rt
!1 DATE PK06LEh1 ~41f0ENC . : EO IVE 7lAM ME7viBERS EACCqt2NTfA6LE PDC.A TWE LINE
35 020a192 THE COOLING TOWERS ARE REPEATED REPAIR COSTS RESTORE COOLING TOWERS TO J. SHARKEY D.
JENKINS P- 2/24i92
DETERIORATING SINCE 1986 RELIABLE OPERATING STATE J. BANDY D 5-18~92
~~ HAVE BEEN USED BEYOND . EVAP L3 (ONE CELL) C 7 26;92
'
f
0 EXPECTED UFE BRINE CHILLER L3 A- 1 2 31 92
; (1
~ r
f
1'/ VACUUM SEAL PIT L1 (ON SCHEDULE)
~
55 4'62 THE TUBES OF THE WIEGAND_ PARTICULATES IN SYSTEM ---
MINIMIZE FOULING OF EVAPORA- -
I. MCLAUGHLIN D. DONAHERi P. 10i92
EVAPORATOR ARE FOULED, - NEED FOR MECHANICAL TOR & IMPLEMENT COST/TIME J. SHARKEY D. SAUNDERS D=
11:92
RESULTING IN INEFFiCIENT CLEANING OF TUBES BES EFFECTIVE CLEANING PROCED- J. BARRINGTON y C C-
02,93
OPERATION URES TO ASSURE ACCEPTABLE I 1 ~ A- 0493
CLEANLINESS OF TUBES
- ~.
lON SCHEDULEi
58 5, 15 92 SIGNIFICANT UNEXPLAINED MONTHLY STEAM USAGE VALIDATE THE EXISTING STEAM D. MERTZ D.
DONAHER P 1 1;92
DIFFERENCES IN STEAM TQ_ Ms USAGE TQMs BY CONDUCTING A RESOURCE: D. SAUNDERS D 1 2-92
USAGE BETWEEN THE THREE . L1 - 2,118,410 LBS/WK ROUGH STEAM BALANCE TO . D. MITCHEM C- 2;93
LINES THAT MAY RESULT IN . L2 858,965 LBS/WK DETERMINE IF & WHERE ENERGY . J. LUSK A- 4 93
ENERGY INEFFICIENCIES . L3 1,780,500 LBSIWK INEFFICIENCIES EXIST AND
THEIR MAGNITUDE
_
61 6/ 1 S'.) 2 HIGH PRESSURE SHOWER . 1992 MONTHLY EXPENDI- REDUCE PUMP DOWNTIME S.KE D. MERTZ P
7r6-92
PUMPS ARE FREQUENTLY TURE ANALYSIS, PURCHASE AND REPAIR COSTS J. DECK D. SAUNDERS D 7~30i92
OFF-LINE FOR REPAIRS REQUESTS G. BALLARD C- 9'10;92
RESULTING IN HIGHER THA_ N . 1992 MONTHLY MACHINE A 1-@-~9-9-Y'
DESIRED REPAIR IR COSTS PARTS - WORK TICKETS INEED PARTS NE`,`+'
SCANPRO ANALYSIS TINIELINE - 1 Z 1 - . 9_i
63 6/29i92 LINE 3 BROKE PUMP IS OVER BROKE PU151P DESIGNED DETERMINE NEEDED IMPROVE- B.
CUMMINS S. SHAKERI P- 10i30/92
SIZED AND RESULTS IN FOR 700 GPM &_ PUMPING MENTS & COSTS TO CURRENT D. DONAHER D. SAUNDERS D- 11
%30~92
EXCESSIVE REPAIR COST & AT 5 GPM L3 BROKE PUMPING TO ELIMI- C- 01.93
OPERATING PROBLEMS DUE . $32,885 REPAIR COSTS NATE PUMP OPERATIONAL A- 06:93
TO CURRENT OPERATING DURING LAST 2 YEARS PROBLEMS & REDUCE REPAIR
MODE COSTS BY 76% YEARLY (ON SCHEDULE)
(LESS THAN $5,000)
61 6 2-t i1: BIRD CENTRIFUGE MAINTE- . UNITS ARE SECOND MOST IMPROVE LIQUOR CLEAN-UP 0. EVERS S.
SHAKERI P 10/30i92
N 4NCE REPAIR COSTS ARE COSTLY REPAIR ITEM IN AND REDUCE MAINTENANCE D. DONAHER D. SAUND_ ERS_ D-
ra
100 TIMES HIGHER THAN VARIABLE REPAIR COST REPAIR COSTS AT THE BIRD C-
?
ALPHA LAVAL CENTRIFUGE EXPENSE CENTRIFUGES A- .~
AND CURRENTLY ARE CLOSE . STA-SIEVES BLIND OVER (COMPLETE - CL 0
TO OPERATIONAL LIMITS ~ n V ~f OUT REPORT \S ~
OF 11/9,321*-'v
t Q,
m
(41n/xl/a:contplan)
9i8Vs4.vzoz

IACTIVEI
PRODUCT/ON DEPARTMENT
CONTROL & IMPROVEMENT PLAN
DATE: 11 09 3;
STAR7 ,
c
::i T£AM 1FEAbEW
. . . .
# DATE PR06LEM L1l1UBNCE ;'. OEJECTIVE TEAM MEE1viBERS ..
CCOUNTA F PDi'.Q.T1ME LINE
66 9/16/92 PARK 500 CURRENTLY IS SHIPPING COST OF $825.00 LOCATE/DEVELOP ALTERNATE P. DUDLEY T.
WEBB P 10i19/92
SHIPPING CONT. DR. BLADE PER NUMBER OF REELS LOCAL VENDORS TO REGRIND D. CLARK W. HAYES D
REELS TO MASS. & OREGON RETURNED TO THERMO OUR CONT. DR. BLADE REELS R, GARG C
FOR REGRINDING, RESULTING_ ELECTRON FOR REWORK AT OR BELOW CURRENT COST A - 3 1~93 ?
IN EXCESSIVE COSTS, LONG . 2 MEETINGS WITH THERMO FOR REGRINDING - $425-$500
SHIPPING AND TURN AROUND ABOUT POOR QUALITY (SAVINGS OF $100,000+) IUPDATE 12'1ti 321
TIME, AND SUBSTANDARD . REEL LIFE DUE TO POOR
QUALITY ON REGRINDS RINDS GRINDS FROM MIDDLE TO
END OF REELS
67 9/18'92 EQUIPMENT LOCK-OUT PRODUCTION DEPART- IMPROVE METHODOLOGY/ R. BRASWELL S.
CLAXTON REPEAT_TQFA AND
PROCEDURES/TRAINING DO MENTAL IMPLEMENTATION SYSTEMS FOR ENSURING S. NELSON B. ESTES REPORT TO
PDMT ON
NOT MEET THE EXPECTA, MOD II TQFQ'S A~ EFFECTIVE EQUIPMENT LOCK- G. JONES 12/1a 92
TIONS OF PRODUCTION OUT IN PRODUCTION AREAS
MANAGEMENT (./~' '
I
1 t
('l ( /
68 9!1 R'92 PRODUCTION DEPARTMENT -FINAL ToFARESULTS- CORRECT EVACUATION PLANS B. SHOPE R.
WILLIAMS REPEAT TQFA AND
SUPERVISORS ARE NOT CNAI+AC- i. AND IMPROVE I-FACTOR BY J. EVANS W. HAYES REPORT TO PDMT ON
EFFECTIVELY CONDUCTING TERISTICS I iMP I i[nF I fACTOR 60 PERCENT 1:r1q 9:
~
EVACUATION TRAINING TO ..............................................................
HOURLY EMPLOYEES, Accuracy I 4 I 3 I 12
RESULTING IN POOR Timey I 2 I 2 I 4
CUSTOMER SATISFACTION Maintenanc_e_ I 2 I 3 I 6
~~ /
AND AN IMPROVEMENT Trainina 2 I 3 I 6
FACTOR OF 28 Understood
" r ..!
~
.
TOTAL - I ( I \ 2~ .
::
" t ..: O ~,
69 9/18;92 PRODUCTION DEPARTMENT -FiNAi TaFARESULTS- TRAIN, THEN DOCUMENT i. MCLAUGHLIN J.
JONES REPEAT TQFA A&e'
DOCUMENTATION AND CHARAO TRAINING FOR EACH EMPLOYEE T. LITTLE W. HAYES REPORT TO PDMT ®I _-s!
TRAINING OF MSDS DOES TERISTICS I IMP I PERF I FACTOR IMPROVE I-FACTOR RATING BY R.
WAGNER 12/14'92 ~ Q
NOT MEET PM USA, NOR ................................................................ 50
PERCENT ~' ~
AUDITOR EXPECTATIONS, c ear Trainirp I 4 I 6 I 20 .~. =
RESULTING IN EMPLOYEES' Accur.Manual_ I 3 I 6 I 16 r .{ t~~
/
~ ,-
LACK OF UNDERSTANDING Compl,Manuals I 2 I 6 I 10 J
r'
OF RESPONSIBILITIES AND Manualg Avsil, I 1 I 6 I 5 J
AN IMPROVEMENT FACTOR
OF 50 To People
TOTAL I I 60 l ~ I~ i
(gn/xI/o:coniplnn)
4TgV64vznz

(ACTIVE)
PRODUCTION DEPARTMENT
CONTROL & IMPROVEMENT PLAN
DATE: 1 1 09;92
^ S7A{tT 7£AM 1 EADr*[i1
l
DATE
PROBLLiVI
:EYlOfNCE
OB.I1rC 1111E:.
TElaM r.1FNE9Eft&
CC~~#CF`f
PfA
3~AE LtNE
70 9/1 8/92 PRODUCTION DEPARTMENT -FINAL TOFA RESULTS- DEVELOP A SYSTEM TO P. PUGLISI 0. HALL P- 1
1/20
/92
MANAGEMENT IS NOT CttARAC i COMMUNICATE REGULATORY D. STEPHENSON W. H4YES _
D- 12,4 92
DELIVERING REQUIRED rEniSnCS I IMP I PEHF I FACTOtI INFORMATION IN A TIMELY B. MA1'ES_ _ C- 12 '1
1'9:
REGULATORY IMFORMATION .r. .-,.....,r .... ............. .... .... MANNER; IMPROVE CUSTOMER
MANNER; A-1 S 93
TO ITS PEOPLE AS PRE- onmun, I 3 I 6 I 16 TOTAL I-FACTOR BY 55 PERCENT
SCRIBED BY FEDERAL/STATE e Comm. I 3 1 6 I 6
STATUES, RESULTING IN aerstooa I 2 1 s I t2
CONFUSION AND A LACK OF ot I 2 I 6 1 1Z
KNOWLEDGE BY HOURLY cation
EMPLOYEES, AND A .
L I I I 6_4
CUSTOMER SATISFACTION
RATING OF 54
71 10/9i92
- - PROD'S CURRENT OPERA- NT RELIANCE ON DEVELOP/IMPLEMENT A SYSTEM
-- B. WYCHE D. MERTZ P- 10/22r92
TION OF ENVIRONMENTAL NGR. TO FIND THAT WILL ENSURE PRODUCTION L. JACKSON D. SAUNDERS D 2 1/93
ABATEMENT EQUIPMENT EMS WI-T-H SCRUBBERS ABATEMENT EQUIPMENT IS W. WILLIAMS_ _ C 3:_ 1,93 ~
WILL NOT MEET FUTURE AIR AND DUST COLLECTORS OPERATED IN COMPLAINCE RESOURCE: Ad. 1 93
EMISSIONS PERMIT STDS., . DUST ON ROOF WITH REGULATIONS IN THE P. PUGLISI
WHICH COULD RESULT IN - REPEAT MAINT.ITEMS ON AIR EMISSIONS PERMIT P. PITTS
NONCOMPLIANCE WITH MONTHLY iNSPECTIONS
THE NEW PERMIT . LACK OF INVESTIGATION OF
SYSTEM FAILURES
NO PRODUCTION SYSTEM
IN PLACE
72 9,13,9 2 PRODUCTION DEPARTMENT 1992 AUGUST COST BOOK REDUCE YTD DEVIATIONS OR B. ESTES J.
NARRON ACT - 12 31 92
CANNOT ASSURE FULFILLING YTD DEVIATIONS PROVIDE EXPLANATIONS TO W. HAYES
FIDUCIARY RESPONSIBILITIES MEET ROC EXPECTATIONS_ D. JENKINS
RELATED 10 1992 SECOND D. SAUNDERS
REVISED BUDGET RESULTING
IN POOR CREDIABILITY IN
COSTCON-T-ROL
74 9/18;92 NO SYSTEM EXISTS TO MAY, 1992 E,S,& H SAFETY ESTABLISH A SYSTEM TO B. VICKERS 0.
AMPEY ACT - 12-31 92
ENSURE PRODUCTION DEPT AUDIT ENSURE TRAINING IS B. MAYES B. ESTES
PERSONNEL ARE TRAINED ACCOMPLISHED & DOCUMENTED
TO OPERATE MANLIFT FOR PRODUCTION PERSONNEL ~
EQUIPMENT WHO ARE REQUIRED TO ' 0
0
OPERATE MANLIFTS a
75 :' 1 S192 PRODUCTION DEPARTMENT . STATEMENTS OF PARTICI- . 100 % COMPLIANCE BY J GLASS LASS D.
JENKINS ACT - 12 :~ 3i
IS NOT IN FULL COMPLIANCE PAN-T-S/"RESPONSIBLES" - MINIMIZE FUTURE AUDIT W. HAYES (q (D
WITH EH&S AUDIT FINDINGS/ . UNFINISHED ASSIGNMENTS FINDINGS/ISSU_ ES_ B. ESTES ~a.
RECOMMENDATIONS AV
(COMPANY POLICY
) ~
WW
---- ~
({lrt/xI/rr.CUntpIan)
sTSvGLvzoz

IACT/VEI
PRODUCTION DEPARTMENT
CONTROL & IMPROVEMENT PLAN
DATE: 11,03 a 2
START
_
:.:.::.
: ...
::.:::; ..::.. ,
:..::.:.:..: : ;...:::. : .::...;::...;.. .
.. .... .
<
F '
# DATE >: ,
Pl{.O8t LM> .. ..... .. ;:;. . ,: ..
TEdMW ;
CGC~ t31 TT~ldH L/~lE
76 9/18/92 PRODUCTION DEPARTMENT . NEW ASSIGNMENTS NOT 100% COMPLIANCE BY 12/31 /92 ~ J. GLASS D,
JENKINS ACT - 12131,92
NOT IN FULL COMPLIANCE PREVIOUSLY MADE -VJ: }#AYES
WITH S. DARRAH'S JOB UNFINISHED ASSIGNMENTS B. ESTES
PROCEDURE PROGRAM FROM EH&S AUDIT
CORRESPONDENCE (CO. . UNFINISHED ASSIGNMENTS
POLICY & RICHMOND EH&S
FROM HIGH-RISK SURVEY ~
REQUIREMENTS) -
( ~
77
1 1/9'92 - - -
SPC SYSTEM REPORT -
-eiNAL TaeA RESULTS- - -- -- ----
IMPROVE TOTAL I-FACTOR BY - - -
B. ESTES
J. NARR bN
ACT - 4'10c93
DOCUMENTATION HAS AN CiiAnAC 50% AND ENSURE CAPABILITY W. HAYFS ;
IMPROVEMENT FACTOR OF TEtaSTiCS i IMP I s'[t+F I FACTOR TO CONTINUOUSLY IMPROVE D, JENKINS
50, RESULTING IN REDUCED ....................... --....................................... THE
QUALITY OF THIS PRODUCT D, SAUNDERS (UPDATE 12 1» 92!
CUSTOMER EFFECTIVENESS Accurecy ~ 3 1 6 I 16
WHEN THIS PRODUCT IS ComPa_te I 3 I 6 ~ 15
USED Ci,rny 2 I 6 ~ 10
L«.ai. 2 I 6 10
TOTAL I I I 60
78 9/18/92 1992 UNION CONTRACT CON- GENERAL LABORERS ARE DETERMINE TRAINING NEEDS C. HARTSELL 0.
HALL ACT--1Z3132
SOLIDATED THE FORKLIFT/ NOT ABLE TO PERFORM AND CONDUCT TRAINING SO D. ORMS B, ESTES
CHECKER AND GENERAL FORKLIFT OPERATIONS IN WE CAN ABIDE BY INTENT OF D. AMPEY
LABORER CLASSIFICATION SPECIFIC AREAS UNION/MANAGEMENT TRNG. GROUP
SOME GENERAL LABORERS AGREEMENT
ARE NOT TRAINED TO PER-
FORM FORKLIFT AND/OR
CHECKER ASSIGNMENTS IN
VARIOUS AREAS
79 1 1;:?;9_ :. HOURLY PERFORMANCE . LACK OF USE OF Q500 . DEFINE BARRIERS & ELIMINATE B. ESTES J.
NARRON ACT --1: 10 93
LEVEL DOES NOT MATCH TOOLS/TECHNIQUES THEM W, HAYES
TOTAL QUALITY NEEDS . LACK OF INVOLVEMENT ON . ALLOW FOR DECISION MAKING D. JENKINS
PROBLEM SOLVING TEAMS AND RISK TAKING D. SAUNDERS (UPDATE - 1 2 14 921
INCREASE INVOLVEMENT
- _ 00
?
80 11 9;92 SALARIED PERFORMANCE . LACK OF USE OF 0500 . DEFINE BARRIERS & ELIMINATE B. ESTES J.
NARRON ACT - 6.'10 ~
LEVEL DOES NOT MATCH TOOLS/TECHNIQUES THEM W. HAYES 0
;
TOTAL QUALITY NEE_DS_ , LACK OF INVOLVEMENT ON . ALLOW FOR DECISION MAKING D. JENKINS O
PROBLEM SOLVING TEAMS AND RISK TAKING D. SAUNDERS (UPDATE 12 Ja
INCREASE INVOLVEMENT fA w
C
All
~
({7n/xUa:c<rntplnnl
0
GievG4vzoz

(ACT-wE)
PRODUCTION DEPARTMENT
CONTROL & IMPROVEMENT PLAN
DATE: 11;03 92
STAftT - .-:
..:..........
: T£4~UI
ll
l~A7e
W~fGE ;:
.,»:: ;
t11 ....... ,,
TEAM M BEfIS ;:;
GfltdNE E
PDCf TIME LINE
81 9/18/92 CURRENT PROD. DEPART. . NUMBER OF SHIFT SUPV. IMPLEMENT A SYSTEM FOR W. HAYES D.
JENKINS ACT 12/1,92
SYSTEM FOR COVERAGE OF WORK-WEEKS IN EXCESS FILLING SHIFT SUPV. VACANCIES B. ESTES
SHIFT SUPV. VACANCIES IS IN OF 40 HOURS TODAY THAT MEETS COMPANY NEEDS
CONFLICT WITH COMPANY . SHIFT SUPV. INPUT AND ADDRESSES SUPV. WORK- (UPDATE - 12 14 9_)
BUDGETARY GUIDELINES & LIFE ISSUES
COMPENSATION POLICY, RE:
OVERTIME, & MAY RESULT IN ~
A WORKLIFE/MORALE ISSUE
AFFECTING JOB PERFORMANCE
AFTER 1/1/93
82 10,12/92 WIEGAND EVAPORATOR SPicSYSTEM - DEFINE & INCOR-PORATE WI-EGAND - J, HANKS R.
BRASWELL ACT 12131 9-;
PARAMETERS ARE NOT OPERATING PARAMETERS AND A. TUDOR D. JENKINS !
INCORPORATED INTO THE STANDARDS INTO SPC SYSTEM
SPC SYSTEM, CAUSING EXAMPLE PARAMETERS: 1 ?''
INCONSISTENT OPERATION . EXIT WIEGAND SOLUBLES (UPDATE - 12 '1 4921 ,
WIEGAND VACUUM ~
STEAM CHEST TEMPERATURE
TURBOFAN VIBRATION
WIEGAND FEED GPM
FINISHER STEAM PRESSURE
83
11r2/92
LOST YIELD OPPORTUNITIES
0 SIB 2% YIELD INCR ASE,
TO TEST THE E CT 0
J. HARK Y _
ONAH -- T~Sfi PLANNED -
& COST EFFICIENCIES MAY REDUCTION IN SLUDGE CENTRIFUGE SLUDGE ON J. HENSLEY D. SAUNDERS 14423=9
EXIST IN OUR CURRENT HANDLING AND LANDFILL FINISHED SHEET SUBJECTIVES, H, WALTMAN
HANDLING OF CENTRIFUGE COSTS BACTERIA LEVELS, & IDENTIFY B. BAILEY 10
SLUDGE PROCESSING PARAMETERS T. BULLOCK
IMPACTED BY THE RETURN RESOURCE:
OF THIS SLUDGE TO THE M. TILLER
PROCESS
(t(n/xI/ae:cc ~itpl~tn)
azsvs4vzaz
